projects
/
wrapfs-2.6.37.y.git
/ commitdiff
commit
grep
author
committer
pickaxe
?
search:
re
summary
|
shortlog
|
log
|
commit
| commitdiff |
tree
raw
|
patch
| inline |
side by side
(parent:
37f7a29
)
ARM: pxa/cm-x300: fix V3020 RTC functionality
author
Igor Grinberg
<grinberg@compulab.co.il>
Mon, 9 May 2011 11:41:46 +0000
(14:41 +0300)
committer
Andi Kleen
<ak@linux.intel.com>
Mon, 1 Aug 2011 20:55:02 +0000
(13:55 -0700)
[ upstream commit
6c7b3ea52e345ab614edb91d3f0e9f3bb3713871
]
While in sleep mode the CS# and other V3020 RTC GPIOs must be driven
high, otherwise V3020 RTC fails to keep the right time in sleep mode.
Signed-off-by: Igor Grinberg <grinberg@compulab.co.il>
Cc: stable@kernel.org
Signed-off-by: Eric Miao <eric.y.miao@gmail.com>
Signed-off-by: Andi Kleen <ak@linux.intel.com>
arch/arm/mach-pxa/cm-x300.c
patch
|
blob
|
history
diff --git
a/arch/arm/mach-pxa/cm-x300.c
b/arch/arm/mach-pxa/cm-x300.c
index d717b49f01725f0adb0c3e3986e7fbc0743d15c2..240455d6ec529a59da52da6f6f0570d9704b5ef4 100644
(file)
--- a/
arch/arm/mach-pxa/cm-x300.c
+++ b/
arch/arm/mach-pxa/cm-x300.c
@@
-157,10
+157,10
@@
static mfp_cfg_t cm_x3xx_mfp_cfg[] __initdata = {
GPIO99_GPIO, /* Ethernet IRQ */
/* RTC GPIOs */
- GPIO95_GPIO
,
/* RTC CS */
- GPIO96_GPIO
,
/* RTC WR */
- GPIO97_GPIO
,
/* RTC RD */
- GPIO98_GPIO, /* RTC IO */
+ GPIO95_GPIO
| MFP_LPM_DRIVE_HIGH,
/* RTC CS */
+ GPIO96_GPIO
| MFP_LPM_DRIVE_HIGH,
/* RTC WR */
+ GPIO97_GPIO
| MFP_LPM_DRIVE_HIGH,
/* RTC RD */
+ GPIO98_GPIO,
/* RTC IO */
/* Standard I2C */
GPIO21_I2C_SCL,